Well, did a little washing, barely made a dent. I think to do it right I need to drop the fuel tank, and then put it on railroad ties.
Washed underneath enough to play with the shift cable, letting it dry before I mess with it.
On a positive note, got a little more sand and gravel in the driveway now.... geeze that thing is packed.
New problems:
1) they cut the chassis harness to wire up a flatbed.
2) I am staring at a 3/8 grade 5 bolt head where there was a bleeder screw. I am not going to touch that yet, pretty fresh Wix metal filter.
3) airbox is not fastened whatsoever. grab ahold and lift it right out.

filter is dirtier than sin, I hope to heck it did not rupture. Needs changed badly.
4) pulleys are making noise, likely need changed.
5) front skidplate is broke, 1/4 of the right side is broke off. Fuel tank heat shield lost its clip at the frontmost location, and the front is bent out a little. RH inner fender has a crack.
6) fuel guage does not work, was not plugged in. Plug it in, still does not work. Unless it is that empty...but the ol back of the hand temp change test told me its about half.
7) antifreeze is not any color in particular. definitely mixed together. Will need to flush with water and change t-stats, as they are for sure stuck open, as it wont barely wiggle past 160 and the top hose is hot.
So, plenty of issues, but it still looks promising for the price.
