Hers what I found out messing with this thing all morning:
1. No.8 wire was burnt again. It was missing the sheild. I replaced the wire and made up a sheild.
2. Compression is good. 140-150 across the board.
3. Timing was off 1.5*. Reset to 4* BTDC with jumper disconnected.
4. Injector spray pattern is consistent on both injectors.
5. Fuel pressure is about 40 psi at the filter. I used a hokey hose and clamp set up to get this. Filter is clear.
6. Firing order is correct.
7. This thing still runs like crap.
8. EGR is clean and appears to be functional. It is electric, so I can't see what state it is in when running.
I tried to upload a video without success... basically, idle is fairly smooth and acceleration is normal in neutral. Once in gear, motor shakes pretty good. Once underway, I get stuttering and pops through the throttle body on acceleration.