Made sure the eprom was seated well, removed it reseated it. I tested the fuel pressure and it was about 5psi before the IP. I changed it with one I have that was getting 10psi. tested and really did not notice any difference. Then changed oil and filter. Cleared codes and it ran perfect. Weird, have not really done anything. No RPM issue. Normal power.
So pulled new codes:
51 PROM Error (Faulty or Incorrect PROM)
53 System Voltage High
66 3-2 Control Solenoid Circuit Fault
67 Torque Converter Clutch (TCC) Solenoid Circuit Fault
78 Wastegate Solenoid Fault
On this drive I came to a full stop. Went FOT, black smoke, good power, seen better. Did this a couple times. The amount of smoke you should normally see from a diesel pulling. I don't think it was excessive. When I get the scan tool I will have a ton more info and probably get it where it should be.