About a week and a half ago, I got the Moose IP from the Tahoe installed on this truck. Since then, I've been working on installing a different (hopefully more sophisticated) electronic boost controller in the truck to control the aneroid, so in the meantime I've had the aneroid backed all the way off so it's allowing full fuel all the time. I definitely have to watch how and when I apply my right foot because it will sure make a smoke show. Even at light throttle this thing is so much more responsive than the old pump I had on. That old pump didn't have any response and was slow to spool the turbo. It's nice to have some pep now.
I've been having some issues with the line for my mechanical fuel pressure gauge losing antifreeze between the isolator and the gauge. I didn't discover this problem until after I put the Moose on and changed the regulator to 25psi. With the old regulator at 5psi I just thought the pressure was too low to register on the 100psi gauge I'm running (excessive, I know, at least for now). So last weekend I took things apart and filled it full of antifreeze again. After that I had a solid reading in the cab, but I didn't drive it since I was still working on installing the boost controller. Two days later I went to drive it and it was only reading 20psi on the gauge and then the next day was 15psi, yet the gauge at the regulator itself was still showing 25psi, so it's still leaking....gotta figure that out. I say this because I'm really curious if my fuel supply upgrades I made have allowed the Raptor 100 to keep up with this IP now. So far I THINK they have because the fuel pressure gauge is reading rock solid even though it's at a lower number, but that's certainly not conclusive. I also say this because now this thing makes black smoke all the way through the rpm range and it didn't do that before, so that also tells me it's shoving more fuel to the injectors than before. On the flip side of that, it will only make about 29psi of boost. Before, when I swapped from the Donaldson air filter to the AFE it jumped from 27-28 pounds of boost immediately to 32-33 pounds of boost. So either the intake I've installed that now has 2 90* turns in it (with one being a Donaldson cobra head) is too restrictive, or the porting I did to the heads is allowing air to flow through the engine better, because everything else is the same as it was on the Tahoe. I'll pull the air intake off at some point and test that.
It's running pretty good though. I need to get the boost controller working so I can tune the rate at which the fuel gets delivered. I used to launch the Tahoe at about 6psi in 2wd and that was about the limit of traction. I figured I could do more with this truck since it's a dually and heavy, so I tried 10psi. It did this instead. And it would have spun them for longer, but I had to get out of it so I wouldn't hit the barn. I sure wasn't expecting this heavy truck to do that.
That's the good news. Now the bad news. Before I took that picture, I was driving the truck around and beating on it, trying to observe boost and smoke at rpm. I made a stop at the grocery store and when I came out there was a puddle of coolant under the truck when I came out. Hmmmmm. I popped the hood and it was coming out of the overflow. Interesting. It was in the 60s outside and the engine hadn't gotten above 175 (which in itself is interesting since I'm running the supposedly "good" Delco 195 thermostat). When I got home there was more coolant coming out of the overflow, in fact you can see it in the picture above. This doesn't feel good. Overnight, I thought about it and convinced myself I have a head gasket leaking at higher boost or a cracked head. Bollocks. I checked my coolant level the next morning and it was exactly at the Full Cold line. Ok, maybe it was just overfull? I recently had a leak at one of the rear block-off plates and I hadn't really driven it much since then, so maybe it was still just overfull. And I cranked the engine and it wasn't hydro-locked, which I was afraid it might be if the cooling system was that pressurized. Hmmm. I picked up a combustion gas tester from Napa to see if that told me anything. During that drive, I hammered on it some more. Yep, more coolant came out. I can't think of anything else that would cause coolant to be pushed out like that now that I'm running more boost than before, when I didn't have a problem at the old boost levels, but I figured I should still test it. The fluid didn't turn yellow, but it definitely wasn't blue anymore.
So the top end's coming off. I'm going to have the heads pressure-tested and if they're good, machined flat. I skipped that step last summer because at that point I was still in a rush to try to get the truck together for camping (which I ultimately never achieved anyway), so shame on me. Hopefully the machine shop can turn the heads around quickly because I'm supposed to take the truck to Dinosaur Camp at KOS October 14-16, so that doesn't give me a lot of time to get it back together and sorted out, plus we're going on a vacation for 4 days before that, so even less time. Oh well, it is what it is at this point.