6.5L
Old Iron Runner
I hope this doesn't get moved. I want some people to see it. Two weeks ago my clutch line decided to kick the bucket. So replaced that, the slave, and the master. Bled the system. Drove it around for a day and a half and then the clutch would not dis-engage. I would pump the clutch for a few minutes to try to bleed some air with no luck. Then would bleed the system again. It would work great for a little while then would start its shit again. So we would bleed it again. Work great. And repeat procedure from then until now. Wouldn't dis-engage at all today which left me driving around town and not being able to take it out of third, which did leave some nice clouds at red lights haha so we bled the system. Works great now. Maybe this is the ticket time it works now for good, maybe it won't, who knows. I suspect air may be getting into the system but I dont know from where. I assume if there was a leak in the system, that when put under pressure would leak fluid and there isn't. Has anybody else experienced this or know what is going on?