Got it started today after many attempts. It ran awful for quite a while.:sad: The raw fuel smoke was so thick in my shop that you couldn't see your hand in front of your face. It spit a bunch of acorn shells and insulation out the tailpipes.):h It smoothed out some after holding at 1500 rpm for 10 minuites or so. Still has a miss:sad: A rear brake line blew out when I backed it up so the exhaust was outside. Tach quit working after 20 minuites of running. Also seemed to be charging rather hard. I'd guess the alternater is as good as dead.All and all ,not the best day.
I had dumped about 4 gallons of fresh fuel and a bunch of power service in with the less than 10 gallons of old fuel that was in it. I don't think the fuel is causing the miss. At this time I'm thinking that the new rings in #7 cylinder are not seated. As said ,the miss got better.maybe it will be fine with some more running time.
Any thoughts? I know I rolled the dice on this one because of the less than perfect cylinder. Just not ready to give up just yet. I did just get a new compression tester a few weeks ago, so after running some more if it doesn't clear up it'll be getting tested.