I read somewhere about 3 years ago, that there is a main valve that controls the flow to both the forward and reverse valves. If that solenoid dies after heating up, that valve will close, causing the transmission to be disabled. I just can't remember where the heck I found that, but I'm leaning...
Yep, it's a HF High End POS. It hasn't failed me yet. I carry my Gold Plated Fluke and a load tester in the pickup for service calls.
The new alternator seems to have a 13 v+- output.
I'm almost there. So far:
Fabricated a complete floor in the cab.
Rebuilt the seat.
Rebuilt the hydraulic...
That's a good idea. Fabricating a barb or something to the base of the AC for a hose is something I can do, until I find the original unit. Interesting note on 427. Is this something I could ID through the VIN, or would I look for a number on the block?
MrMarty, it had no output. Bought a reman. Now between 15 and 16. Battery charged right up. Now I'm down to a seal in the steering pump and some breather lines on the valve covers.
Thanks Will L. 150k miles start, 200k stop. Bought it in 6/2012. Parked it in 2/2015. Some towing, rarely heavy. Was strong till the day of fate. Aeration possible. Filter and seal were new, but will check for tightness when pan drops.
Hmmm,,, That is really good advice I wasn't even asking for. I also thought the air cleaner should have been bigger. I was almost ready to cut that threaded cover rod. Your right about trash getting into the valve cover. That's got to be fixed. I just picked up a Shop Manual Supplement...
Thanks FellowTraveler. A rebuild kit was my first choice, but I couldn't find one. Wasted money trying a generic kit. Anyway, I got it figured out. The final retaining plate was not fully seated. I tapped it in until it was tight and like magic, no more leak. I would bet the 2 before that, had...
I had a problem with a 4L60E transmission a while back. Up until the day it failed, I drove it without an issue. Then one day, I went to a convention in Orlando FL, about 40 minutes from the house. I parked it and went inside. When I came out. I hopped into the truck, started it and drove out of...
Thank you WarWagon. It was not charging the battery so I replaced it with a reman. Haven't started it to test yet. Had to patch a rust hole in the big fuel tank. It's been one thing after another with this old rusty truck, but I think I'm finally turning the corner with it. Love that JB weld...
The problem is solved. The seal/spring retainer plate was not properly seated. Tapping it tight DID fix the problem. The fluid flowed through, back into the reservoir with no sign of leakage from the HB. So the last three returns to AdvanceAParts were probably good. I'm glad I found it, but what...
Ok folks. The problem is solved. The seal/spring retainer plate was not properly seated. Tapping it tight DID fix the problem. The fluid flowed through, back into the reservoir with no sign of leakage from the HB. So the last three returns to AdvanceAParts were probably good. I'm glad I found...
I know. That's a good question. This is a Pretty big truck. I'm really guessing here, so don't hold me to this. The HB provides the main pressure source and the Power Brake Booster vacuum serves as a backup in the event something goes south with the fluid pressure mid stride. It's an ole 86...