Okay so check this out. I stripped the intake and throttle body to clean it all up. When I took the throttle body apart from the little riser I found the probable cause of the skip and labor knocking.
Yes. I managed to blow a head gasket one morning on the way to work. Had a young man, high school age, riding my ass and no matter what I did he wouldn’t back off. So when he finally decided to try and pass I hammered down and the result of that I developed a skip. Kept driving the truck with it...
It crossed my mind to that😂 thank you for that info. Definitely an easy fix relocating the filter. I just pulled the heads in record time, for me anyway. 3hrs.
Nothing on this truck is original. It was put together from other vehicles.
Thank you for your input. Is that adapter something I can pick up at a parts house or is something more likely to be ordered offline
The truck is on a 4x4 chassis equipped with transfer case, front differential, and a brand new complete front end suspension. When I bought the truck the guy said the front drive shaft for the four wheel drive needed a new U-joint and he had taken it out. After crawling under the truck I...
Alright guys I’m here for ideas, advice, and knowledge I may be lacking in. I have a 1988 GMC short wheelbase pickup. I bought it from a guy who said “it’s one we put together”… it has the 305cid 5.0L TBI bolted to a THM700-R4 transmission bolted to a four wheel drive transfer case. The title...